Power certainly did drop, fortunately being a hot day there was plenty of lift about. I had fresh 98 in it, and then put some fresh 100LL in it.
Filter is clean. Float bowls clean and correct levels. CHT was normal for the weather, EGTs may have indicated differently if they were fitted, but this installation has none.
I didn't even think of that, but probably because there were no weird noises when turning by hand.
I have experienced this also, but only at idle. Float bowls were checked immediately after shutdown when the abrupt power drop occurred on ground run. No anomalies were found.
I thought that also and the carbs and fuel system were the focus of my troubleshooting. Cables and stops have been checked and rechecked. Slides, diaphragms, needles and spring lengths checked and rechecked also.
Everything seems to point carbs or induction.
I'm just about tearing my hair out because I can't find a solid fault and I was planning to fly out at first light.